The centres for the tines were marked and the holes drilled with a 11/16 th brace bit (1/16 th less in diameter than the tine size). These were carefully drilled perpendicular to the base (drilling from both sides) and then adjusted to obtain a tight fit. I decided to drill right through for strength and then use hardwood wedges in the top to prevent movement.
Before drilling the holes for the stail, I decided it would be better to fit five tines around the centre to prevent any tear-out in the tine holes. This was straight forward by checking the fitting of the tines and knocking them into place after sawing a slit for the wedges, sawing them to the correct length and finally hammering in some hardwood wedges and trimming. They were not glued. The ends of the tines were also shaped.
The stail was connected to the head by drilling two 5/8 th inch diameter holes right through the head. It is important to get two correct angles: a) the angle of the stail "prongs" going into the head. I calculated this as 7 degrees from the perpendicular, b) the angle to give the head a slight tilt forward so that the tines point backwards towards the user. Because the stail was already curved to the ground at the rake end, this angle (normally adjusted to about 75 degrees) was left at 80 degrees so 10 degrees off perpendicular. I think 75 degrees would be too steep an angle for a garden rake.
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The stail and head joined with the tines in the centre in place. |
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Finished rake after treating three times with linseed oil. |
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The tines were shaped ready for use. |
As this was my first try at a rake, I'll make a few comments on the method and how it could be improved:
1. The teeth could be made slimmer so there is more leeway in fitting the stail to the head. However, they are going to get the brunt of the action in the garden and need to be a good size and held firmly. Some designs actually use nails as tines.
2. My stail was slightly curved to start with and it would have been better to steam it and try and straighten it, However, as the wood was green, I clamped it straight whilst it dried and that worked well.
3. A rectangle mortice/tenon might be easier to do than a cylindrical one because of the complex angles involved. I found this stage the most difficult.
Hopefully the rake will last a long time. I'll update after some use!
Some notes on historical designs.
A good source of information on hay rakes is a chapter in the book by Drew Langsner "Country Woodcraft" Rodale Press, 1978. This chapter covers several designs including a rake design from Finland that is very different from the English design that I have been describing. He states that the best tines are from cleaved straight-grained hardwoods such as oak, ash, beech. hickory, locust or mulberry (author lives in the USA) and the Finns traditionally use lilac.
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A hay rake displayed in Gimmelwald, Bernese Alps. This is a different design from those I have seen in UK. It has three bow stays to hold the head in place (some are broken) and it looks like the stail (shaft) has been attached to the head with a metal plate, probably as a repair measure. It also has about 24 teeth which is a lot for a hay rake (normally around 15 on a 28-inch head, Tabor, 2000). |
Second rake - a hay rake.
Hay rakes are generally wider, have thinner tines and also a longer handle, I decided to have a go but this time using alder poles for the stail but sticking with hazel for the rest. Alder was used in the past I think and certainly for scythe handles.
I started by getting three poles from a sapling in a nearby coppice. I expected the upper portion would be too thin for a stail but would make a useful stake for the garden.
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Coppice of alder and hazel. |
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One sapling but three 6 ft poles ready for debarking and shaping with the stail engine. |
I used the draw knife to remove the bark and smooth knots. On the two wider poles it was possible to shape the poles to reduce any curvature. The use of the stail engine has been given in another BLOG post so I will not repeat that here:
Construction of a Stail Engine. Basically, the more I use the stail engine, the more I get to know how to set it up and get good results; it is definitely a bit of an art to operate but it is good fun once mastered.
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The poles drying after rounding and one of the poles was split ready for mounting on the head. The other one will be stored for now. |
I chose the middle pole to split about 21'' inches from the bottom and put a thin stainless-steel strip around to prevent further splitting. The strip was held in place with two galvanised nails. The other pole will be dried and kept as a backup. Later, when bending the bow stay, I placed the stail inside the steam box for 1 hour and after steaming bent the rake end of the shaft to give it a curvature of about 20 degrees. This will allow the stail to be inserted into the head at right angles.
The 15 tines were made from seasoned hazel by chopping to size (about 7 '' long) and then using the rounding planes to get to 1/2'' diameter as described above.
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The 1/2'' rotary plane in use cutting a tine for the rake head. Larger diameter planes were used to reduce the size to get the 1/2'' plane to fit. |
The rake head was made from a trunk of hazel that had fallen in a storm and was partially dry.
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The mixed woodland containing hazel, ash, pine and field maple where the hazel pole was obtained from a fallen trunk. |
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The 30'' hazel tree trunk used to make the rake head |
The head was made by using the froe to cleave four sides to start shaping. Then a flat face was chosen and prepared by a combination of cutting with a draw knife, roughing plane and wooden fore plane. The surface was made flat and winding sticks used to ensure a minimum of twist. Once a good face had been prepared, this was used to mark a cutting line on the opposite face to give a width of 1 3/4'' and then sawn with a rip saw using the guidelines to keep the cut true.
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Marking the rip-cut line with a kerfing plane. |
The shape of the head was then finished by sawing and shaping with the fore plane and jointing plane. The head had a slight curvature, shaped with a large spokeshave, from about 4 cm at the ends to 5 cm width in the middle. The tine positions were then marked along a centre line and 2 inches apart giving a total of 15 tines. The holes for the tines were then drilled using a tradition auger 1/2 '' bit from the top of the head through and then finished by drilling from the bottom of the head.
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It is important to get the right levels when drilling at right-angles to the head. I did this using a straight guide and small set square. |
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The rake head after shaping and drilling the holes for the 1/2'' tines. |
Making the Bow Stay.
This rake was wider than the garden rake and so for added strength a bow stay was used to reduce the leverage on the central fork. Some hay rakes have the stail mounted directly into the head without splitting and use a bow stay to stabilise it. I think a more robust method is to retain the fork and split stail and add a bow stay (or even two).
To prepare a bow stays I found ash and hazel saplings about 2 m in length and about 3/4 '' in diameter and rounded them down to 1/2'' diameter with the rounding plane and then left these to dry. I will choose one of them after I have tried bending. They were not supple enough to bend without breaking and would need to be steam bent into shape on a former.
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The ash and hazel bows ready for steam bending. |
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Steam box with saplings inside. The box is about 2 m long, made of pine and coated on the inside with polyester to help protect the wood from water. |
The steaming took 45 minutes with the steam fed in the middle on the top and two drain holes near the ends at the bottom. The steam was generated using a standard wallpaper stripper.
After steaming the saplings were bent on a former as shown.
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The rods on a former after steaming and left to cool to get the correct shape. |
The hazel rod worked best, mainly because it had fewer knots. The rod was obtained from a six-foot length of hazel (chosen with minimum knots!) about 1 inch in diameter and turned down to 1/2 '' for the stay before bending. It was not dried but still green when it was bent. I did try shortening the steaming time to 20 minutes, but the wood was still too brittle to make a tight bend. I found that the green wood was not supple enough to make a tight bend and some steaming was needed.
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