We found this buried in our allotment and it seemed a shame not to put it back into use. This tool did bring back memories from my child hood in Norwell Woodhouse (a hamlet in Nottinghamshire) when my father made one from a garden fork and we used it to rake the ground and break-up clods of earth after digging the garden. As the soil often needed working to get a fine tilth for setting seed, it was useful for breaking up larger lumps. Sometimes he ploughed the garden and then it was a good tool for breaking and levelling the furrows.
![]() |
The drag fork and collar before treatment. |
The stem of the fork (or tang) for mounting in the handle was relatively short and the tool that we found had a long collar to strengthen the joint. Unfortunately, the joint had proven a problem as there were several nails hammered into the wood inside the collar to tighten the fit. I decided to shorten the iron collar so that it matched the length of the metal tang and also as the top of the collar had been badly beaten, this was sawn off to give a uniform cross-section.
The fork and collar were cleaned with a wire brush and treated with phosphoric acid to reduce further rusting. They were then treated with Hammerite black paint and left to dry.
The shaft was made from hazel taken from our boundary hedge. This was about two inches in diameter. As it was cut in the summer, the wood was heavy and very green.
The piece of hazel used to make the shaft. This was about 48 inches long and 2 inches in diameter with a slight taper and a couple of knots but it did have a slight curvature that could be utilised in the design. |
The bark and knots were worked with a draw-knife and some wood removed where the stem took a slight elliptical cross-section. This was further improved using a stail engine (adjustable rounding plane) in one pass. This was quite difficult because the wood was wet and stringy but with some perseverance it did work. After this it was left to dry before using the rounding plane to reduce the diameter to 38 mm (about 1.5 inches) ready to reduce the end further for the iron collar.
![]() |
The hazel shaft after one pass of the stail engine. |
The method of fixing the fork tang to the handle proved quite tricky as the previous attachment had been a failure judging by the number of nails hammered into the shaft to keep the fork attached. This was because the tang was relatively short and even with the long iron collar the leverage encountered in use was liable to be pulled out from the shaft. The method I used will hopefully overcome this but only time and use will tell.
I reduced the bottom 84 mm of the shaft to a diameter of 32.5 mm by sawing a groove at 84 mm from the end and sawing around the circumference only deep enough to get the reduced diameter for the collar to fit. After sawing the limiting cut, I then used the stail engine to reduce the diameter as needed, finishing the cut using a carving knife. The final fitting was done by inserting the collar as far as possible and noting the tightness before filing with a fine wood file around the circumference. In this way I got the collar to fit tightly on to the shaft.
Having fitted the collar, the next job was to drill the centre hole for the tang. The tang was rectangular in cross-section (10 mm wide by 8 mm depth) so I chose the nearest auger drill size (#5, 5/16 th inch diameter). The collar was left in place to strengthen the wood whilst drilling.
![]() |
The arrangement for drilling with the auger drill. The winding sticks were used to keep the drill in-line. |
As it is important to make the tang-hole central in the handle, care is needed to ensure the hole is in the centre of the tang-attachment portion, particularly as the handle is not straight in both dimensions as will be shown later in the photos of the finished tool. Hence the use of a spirit-level near the tang- attachment portion as shown above. The depth of the hole was measured to include the straight and curved part of the tang to get as much as possible of the iron into the shaft. The hole was then carved to a rectangular profile using a 5 mm chisel and the #5 auger bit to clear-out the waste wood. The end of the shaft where the tang curved, a channel was carved to accommodate the tang. The tang was then pressed into place and the hole carefully filed to get a very tight fit. A modification was also made to fit a small bolt through the collar, shaft and tang that involved drilling a 4 mm hole with a high-speed metal drill. Finally, the end of the shaft was sealed with epoxy resin to help protect the end-grain from water and further aid the secure fixing of the tang.
![]() |
The attachment of the shaft to the tang showing the collar, through bolt and resin on the shaft end. The external diameter of the collar was the same as the shaft. |
The shaft was then scraped and sanded ready for treatment with oak dye and linseed oil.